I had to make modifications due to space constraints and being an idiot that got the wrong fittings. Didn't realize the 1" sharkbites I got only worked on PEX so could not bridge to PVC. I did have the right ones to bridge from pex to pvc in 3/4. So I used a reducer. used 1-1/4" rigid conduit elbow to bend the 3/4" pex (I got it in white instead of blue or red). It was a bear getting the pipe to come out the other side of the conduit but once it did, it moved much more smoothly and was much easier for my friend to bend in place.
This is the view from outside the shed:
I cleaned off the cistern lid. The blue corrugated stuff behind the bucket is the main line into the shed. It goes into a weatherproof junction box inside the cinderblock and comes out as the weatherproof flexible conduit that you can see scraps of in the bucket. Sadly, that flexible stainless steel hose thing didn't work-- leaked like crazy. The shed itself is obviously rusting badly.
When we replaced the old bad liquid level float switch we couldn't find the same type and the old one had a piece welded on to it to extend the tongue. The new one could not mount directly to the top of the PVC and if it had, it would not be able to reach the hole. The well repair guy initially glued the wooden block down to the lid of the cistern and screwed the switch to it, but the block wouldn't stay still. It kept moving and the lever kept jamming and the cistern overflowed multiple times. I intend to add couplings and run conduit all the way down to the float switch and use some threaded adapters to go from the 3/4" to 1/2" that will fit in the holes on the switch. For the elbow coming out of the outlet box, I will run more conduit with 12/2wg outdoor rated cable to have a 15A GFI outlet. There will be an in-use weather cover over the outlet as an extra precaution. The white cord from the LED strip light will be plugged in to it.
I managed to patch the hole in the ceiling right above the switch with some Flex Shot spray.
Finally ended up moving the block to the pipe, notching the front of the block to allow the rod to move unobstructed. I wish I had something to keep it more straight up and down though. It still sticks sometimes. Really want to replace that with a different type of sensor at some point in the future. I'm hoping that I can find something that can run off of the same breaker as the actual belt-driven pump that fills the cistern. That thing runs on 230V so I need something compatible.
View to the left when stepping in to the pump house: I'm pleased with how the conduit looks and am glad we found something sturdy to go through the holes that were drilled in the I-beam. We ran out of cable and I've decided that the last run that is missing (on the left) will be the 12/2 since it only needs to power a couple of outlets. I have since closed the sub panel.
The walls are rusting away so I'm going to have to hit them with Rustoleum temporarily but I'd like to eventually build a wooden shed around the metal one and then remove parts of the metal one that are not needed. I want a larger shed with storage for plumbing supplies, insulation, and doors that aren't broken off.
You can see a little of the new pipe (the vertical loop is the new 3/4" PEX) and you can see the pipes for the belt driven pump.
Cable going from the float switch to the belt-driven pump and the coupling that will connect conduit for the GFI outlets. White pipe is just spare pipe that I need to store better.
Upper view from north side of the shed: the ugly tangle of useless cables is gone.
Here's where it gets ugly. LOL. Got the
The 90s probably don't help the water pressure any. Comes out of the tee to the right, goes up and around and down to the PVC tee that was there from a previous fix. I wanted to add a shutoff to just the house water but the kind I had would not fit. If there are problems in the future I can probably add one in to a vertical run of the pipe going down into the dirt.